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Old 09-12-2017, 07:44 PM   #42
kuntzbros
 
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Name: kuntzbros
Title: Green Behind the Ears
Status: Not Here
Join Date: Jun 2017
Location: Jefferson, GA
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Posts: 34
Bad news on this update. After a good and consistent performance at the roadkill ziptie drags we decided it was time to give the truck some more fuel. We picked up a mac rack plug from Powerdriven that takes the rack travel from 19mm-21mm to give us a little more fuel at full throttle and maxed the barrels. We also have a friend that has a general industrial machine shop so in search of more fuel we had him take the stock delivery valves and grind them down from 8.0mm to 7.5mm. He couldn’t take it any farther or he was going to start hitting the top part of the delivery valve if he went any further. After talking to Will at PDD he informed us that while not technically full cut dv’s, taking .5mm (.020”) off would yield as much fuel flow as a full cut.

We then made our way to the local drag strip test and tune and were excited to find out how much more power we squeezed out of Lildebbie when unfortunately, on our first pass we had a small but very bad malfunction. After pulling a much improved 60ft time, at about half track something went terribly wrong. A faulty and very old radiator cap could not hold anymore and blew off into the overflow which then filled and blew off almost directly in front of the passenger side front tire causing essentially an oil slick and causing the truck to lose control and slide across the track sending it head on into the concrete wall. While no one was physically hurt the same could not be said about Lildebbie. With both frame rails bent and motor and trans mounts broken the truck was towed off the track and winched back up on the trailer.

http://www.youtube.com/watch?v=RDSdl...ature=youtu.be

bent frame rails 1.jpg

bent frame rails 2.jpg

lildebbie front end.jpg

sideways bumper 1.jpg

sideways bumper 2.jpg

snapped motor mount bolt.jpg

Once we got the truck home we found that the motor would not run and did not want to turn over freely. After checking all the simple/easy things the only thing left to do was to pull the motor. After only being in the truck for a few months we reluctantly pulled the motor and started to disassemble. During disassembly, the news began to get even worse not only was the truck totaled from the bent frame but the connecting rods were bent and to make matters even worse the 1st cylinder was cracked almost from top to bottom between the 1st and 2nd cylinder thus essentially making the motor also totaled.

bent connecting rod.jpg

broken cylinder.jpg

#lildebbie was taken from us way too soon. We know her legacy cannot die here. Hopefully we will be able to find another truck and continue in the name of #lildebbie
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