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Old 03-19-2018, 08:33 PM   #26
97rada
 
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Name: 97rada
Title: Too Much Time
Status: Not Here
Join Date: Feb 2008
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Posts: 5,410
Quote:
Originally Posted by Big Blue24 View Post
This event was the very first passes with the fresh engine and trans setup. We are trying to be better prepared for UCC this year and possibly chase Super Street points in the NHRDA.



First pass a -12an fitting on the Waterman lift pump vibrated loose spraying fuel everywhere. Also had a turbo drain fitting come loose from the block and spray a little oil from escaping crank case pressure.



Second pass the RPM trigger on the controller for the shift noid acted up and short shifted the truck. It also had some violent torque steer at the hit.



Third pass, the tierod bent down several inches presumably at the hit and truck went violently toward the wall, popped the Hoosier Quicktime Pro tire off the passenger front bead and Todd narrowly missed the wall. The rim scratch path on the track came within inches of the wall.... great save!!!



We got some data, fixed a few gremlins, had great success with the transbrake setup on both trucks and it was a great test n tune.... for UCC!



Probably need to upgrade the tierod assembly, beadlocks or similar for the front tires, maybe a few other upgrades! What's neat is we were able to spool up fuel-only with the DPC slut converter despite the large GTX55 on the manifold fed by 2 more GTX55's. We decreased the engine displacement, cam size, and War Head flow a bit on the new engine setup, but still making excellent power!


Pictures of the setup? Sounds like enough air for stupid power
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Austin
tow truck- 14-3500 with tuning
toy truck -94 rclb auto- 5.2x with a lot left. Shooting for 4s

Any intelligent fool can make things bigger and more complex...it takes a touch of genius- and alot of courage to move in the opposite direction.
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