Advertisement |
|
|
|
If this is your first visit, be sure to check out the FAQ by clicking the link above.
You may have to register before you can post: click the register link above to proceed.
To start viewing messages, select the forum that you want to visit from the selection below.
|
6.0 Powerstroke Discussion of the 03-06 6.0 |
11-25-2015, 03:51 PM
|
#1
|
Name: 808cummins
Title: Green Behind the Ears
Status: Not Here
Join Date: Apr 2009
Member`s Gallery
Posts: 69
|
Injector issue HELP PLEASE!!
07 f250 just recently done mkm customs kit (studs gaskets etc) for about 3 days, truck ran fine. This morning truck sputters and ran rough. Almost no power at all. I got a cylinder 3 low contribution code. Opened up valve cover and noticed the injector bolts on that whole bank was hand tight so now cyl 3 and 5 injector seals was trashed! I got access to new seals (copper washers) AND injectors. The thing is, what are my chances if I just changed the seals and install my original injector and the truck runs fine? I don't want to install it to find out injector might had been damaged also. I did a buzz test on all four and they are working. But I've been told that's only on the electronic side
__________________
06 dodge, crazy larry file w/outlook stacked with power puck, quadzilla boost fooler, custom intake, 4" aero exhaust, ATS billet transmission with converter lockup switch, heater grid delete, 12" of lift w/39.5x13.5x20 irok radials on 20x12 weld cheyenne's
|
|
|
11-25-2015, 06:16 PM
|
#2
|
Name: will24
Title: That guy
Status: Not Here
Join Date: May 2010
Location: South Williamsport, PA, Elverson, PA and Luray, VA
Member`s Gallery
Posts: 2,719
|
Swap the seals and washers and torque to 31 ft lbs. the injectors will be fine. My sloppy coworkers would fail to torque an injector once a week, I always got the rework and the injectors were fine. I'm impressed that it ran though, usually you get a no code no start with in spec icp when the washer blows out
Sent from my flashscan v2
__________________
|
|
|
11-25-2015, 09:39 PM
|
#3
|
Name: Bad Moose
Title: Just a pain in the arse
Status: Not Here
Join Date: Oct 2008
Location: Kansas
Member`s Gallery
Posts: 921
|
X2 on the injectors being fine.
__________________
'03 F250 King Ranch
Custom tuned SCT X3 by Eric at Innovative
3.5" DP into 4" AFE exhaust
Airraid filter
Edge Evolution for gauges
EGR went bye bye
|
|
|
11-25-2015, 10:59 PM
|
#4
|
Name: 808cummins
Title: Green Behind the Ears
Status: Not Here
Join Date: Apr 2009
Member`s Gallery
Posts: 69
|
Awesome! I'm glad to hear they will be ok. As soon as truck ran rough, I pulled over and probably tried to get her running I'd say 3 times before I decided to stop and tow her home. It's not like I tried to push it miles before I called it quits. I'm pretty sure this was installation error cause 1,3,5,7 injector bolts was barely tight. I opened up driver side cover and all injector bolts was tight. Big thanks Will and moose!
__________________
06 dodge, crazy larry file w/outlook stacked with power puck, quadzilla boost fooler, custom intake, 4" aero exhaust, ATS billet transmission with converter lockup switch, heater grid delete, 12" of lift w/39.5x13.5x20 irok radials on 20x12 weld cheyenne's
|
|
|
11-28-2015, 10:56 AM
|
#5
|
Name: vinniehobart
Title: Diesel Enthusiast
Status: Not Here
Join Date: Apr 2013
Location: Valley Center
Member`s Gallery
Posts: 151
|
make sure you clean the injector cup. just like doing a 7.3 injector swap. pieces of copper washer may be stuck to the bottom
__________________
2003 Ford 6.0 CCSB Lariat Gearhead Tuning,S362FMW 62/68/.83,Driven Diesel, Irate Diesel, ISSPRO, S&B. 493 fuel 541 on
2006 F250 6.0 single cab gearhead tuning SX-E S369 RCD 250/150 injectors, Thumper 2, stock 224k mile trans!! 7.90 @89MPH!!
|
|
|
Posting Rules
|
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts
HTML code is Off
|
|
|
All times are GMT -5. The time now is 08:07 AM.
|